Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine

Currently, the Southern Illinois University Carbondale (SIUC) power plant produces steam at high pressure to drive a high pressure (HP) turbine to make a portion of the electrical power needed by campus, then using 969 kPa (125 psig) steam to provide hot water all year, heat buildings, and to operat...

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Bibliographic Details
Main Author: Su, Heyin
Format: Others
Published: OpenSIUC 2011
Subjects:
VFD
Online Access:https://opensiuc.lib.siu.edu/theses/708
https://opensiuc.lib.siu.edu/cgi/viewcontent.cgi?article=1715&context=theses
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spelling ndltd-siu.edu-oai-opensiuc.lib.siu.edu-theses-17152018-12-20T04:37:55Z Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine Su, Heyin Currently, the Southern Illinois University Carbondale (SIUC) power plant produces steam at high pressure to drive a high pressure (HP) turbine to make a portion of the electrical power needed by campus, then using 969 kPa (125 psig) steam to provide hot water all year, heat buildings, and to operate a low pressure (LP) turbine that powers the compressor of the central air conditioning (A/C) system. In the proposed system, the HP turbine is replaced by a much higher efficiency, multi-level turbine, the LP turbine is replaced with a motor and Variable Frequency Drive (VFD), and a cooling tower is added to condense more possible steam. This thesis has provided computer models to evaluate the economical feasibility of the proposed system, which are written by using Engineering Equation Solver (EES) software. The results of the study are presented in two cases. Case 1 examines the same amount of coal use between current and proposed systems, while Case 2 exames operating the high pressure boiler at the maximum rate. The results are a cost savings of $1,921,000 and $3,604,000 with payback periods of 4 and 2.2 years for Case 1 and Case 2, respectively. The annual primary energy saved and CO2 reduction from this modification was 200,000 GJ and 564,814 moles, respectively. 2011-08-01T07:00:00Z text application/pdf https://opensiuc.lib.siu.edu/theses/708 https://opensiuc.lib.siu.edu/cgi/viewcontent.cgi?article=1715&context=theses Theses OpenSIUC Air Conditioning Engineering Equation Solver Steam Turbine VFD
collection NDLTD
format Others
sources NDLTD
topic Air Conditioning
Engineering Equation Solver
Steam Turbine
VFD
spellingShingle Air Conditioning
Engineering Equation Solver
Steam Turbine
VFD
Su, Heyin
Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine
description Currently, the Southern Illinois University Carbondale (SIUC) power plant produces steam at high pressure to drive a high pressure (HP) turbine to make a portion of the electrical power needed by campus, then using 969 kPa (125 psig) steam to provide hot water all year, heat buildings, and to operate a low pressure (LP) turbine that powers the compressor of the central air conditioning (A/C) system. In the proposed system, the HP turbine is replaced by a much higher efficiency, multi-level turbine, the LP turbine is replaced with a motor and Variable Frequency Drive (VFD), and a cooling tower is added to condense more possible steam. This thesis has provided computer models to evaluate the economical feasibility of the proposed system, which are written by using Engineering Equation Solver (EES) software. The results of the study are presented in two cases. Case 1 examines the same amount of coal use between current and proposed systems, while Case 2 exames operating the high pressure boiler at the maximum rate. The results are a cost savings of $1,921,000 and $3,604,000 with payback periods of 4 and 2.2 years for Case 1 and Case 2, respectively. The annual primary energy saved and CO2 reduction from this modification was 200,000 GJ and 564,814 moles, respectively.
author Su, Heyin
author_facet Su, Heyin
author_sort Su, Heyin
title Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine
title_short Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine
title_full Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine
title_fullStr Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine
title_full_unstemmed Modeling of Proposed Changes to SIUC Central Heating, Air-Conditioning, and Power Plant Incorporating Variable Frequency Drive (VFD) and High Efficiency Turbine
title_sort modeling of proposed changes to siuc central heating, air-conditioning, and power plant incorporating variable frequency drive (vfd) and high efficiency turbine
publisher OpenSIUC
publishDate 2011
url https://opensiuc.lib.siu.edu/theses/708
https://opensiuc.lib.siu.edu/cgi/viewcontent.cgi?article=1715&context=theses
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