Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation

碩士 === 國立中興大學 === 生物產業機電工程學系所 === 102 === The purpose of this study was examining the engine components damaged by hydrogen sulfide corrosion of biogas electricity generation system, and replacing corrosion-resistant materials for them. It cloud solve the problem of hydrogen sulfide corrosion. There...

Full description

Bibliographic Details
Main Authors: Min-Heng Gao, 高敏恆
Other Authors: 雷鵬魁
Format: Others
Language:zh-TW
Published: 2014
Online Access:http://ndltd.ncl.edu.tw/handle/44666390484750273937
id ndltd-TW-102NCHU5415003
record_format oai_dc
spelling ndltd-TW-102NCHU54150032017-01-27T04:12:13Z http://ndltd.ncl.edu.tw/handle/44666390484750273937 Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation 運用抗腐蝕材料於柴油引擎進行沼氣發電之研究 Min-Heng Gao 高敏恆 碩士 國立中興大學 生物產業機電工程學系所 102 The purpose of this study was examining the engine components damaged by hydrogen sulfide corrosion of biogas electricity generation system, and replacing corrosion-resistant materials for them. It cloud solve the problem of hydrogen sulfide corrosion. Therefore the recovery period of equipment should be extended and the maintenance cost be reduced. Diesel engine was modified as biogas engine in this study. The components were replaced by bearing of battitt metal and oil seal of silicone rubber. The system were operated and evaluated in hog farm. Voltage and frequency were measured to examine the quality of electricity. The exit air of engine was evaluated by the concentrations of CO, SO2 and NOx for examining the emission standards. The economic analysis among varied power generation system was conducted. Important results of this study were described as followings: Voltage (230V) and frequency (59.6 ~ 60.6 Hz) were maintained within the power quality standard (220±11 V;60±2.4 Hz). The concentrations of CO2 were measured from 762 to 1,060 ppm which were within the emission standard while the methane concentration was 52.8% of biogas. They were measured from 1,926 to 2,843 ppm which were over the emission standard while the methane concentration was 74.6% of biogas. The concentrations of NOx and SO2 were measured from 626 to 1662 ppm and 103 to 288 ppm, respectively, both of them were over the emission standard(250 ppm and 50 ppm, respectively) under the loading operation of biogas electricity generation system. The equipments were designed for biogas electricity generation which would create 240,300 kWh/year. The results of economic analysis show the investment cost of anti-corrosion biogas electricity generation system have the lowest value as NT 800,000 dollars and the recovery period be the lowest value as 1.5 year. 雷鵬魁 2014 學位論文 ; thesis 77 zh-TW
collection NDLTD
language zh-TW
format Others
sources NDLTD
description 碩士 === 國立中興大學 === 生物產業機電工程學系所 === 102 === The purpose of this study was examining the engine components damaged by hydrogen sulfide corrosion of biogas electricity generation system, and replacing corrosion-resistant materials for them. It cloud solve the problem of hydrogen sulfide corrosion. Therefore the recovery period of equipment should be extended and the maintenance cost be reduced. Diesel engine was modified as biogas engine in this study. The components were replaced by bearing of battitt metal and oil seal of silicone rubber. The system were operated and evaluated in hog farm. Voltage and frequency were measured to examine the quality of electricity. The exit air of engine was evaluated by the concentrations of CO, SO2 and NOx for examining the emission standards. The economic analysis among varied power generation system was conducted. Important results of this study were described as followings: Voltage (230V) and frequency (59.6 ~ 60.6 Hz) were maintained within the power quality standard (220±11 V;60±2.4 Hz). The concentrations of CO2 were measured from 762 to 1,060 ppm which were within the emission standard while the methane concentration was 52.8% of biogas. They were measured from 1,926 to 2,843 ppm which were over the emission standard while the methane concentration was 74.6% of biogas. The concentrations of NOx and SO2 were measured from 626 to 1662 ppm and 103 to 288 ppm, respectively, both of them were over the emission standard(250 ppm and 50 ppm, respectively) under the loading operation of biogas electricity generation system. The equipments were designed for biogas electricity generation which would create 240,300 kWh/year. The results of economic analysis show the investment cost of anti-corrosion biogas electricity generation system have the lowest value as NT 800,000 dollars and the recovery period be the lowest value as 1.5 year.
author2 雷鵬魁
author_facet 雷鵬魁
Min-Heng Gao
高敏恆
author Min-Heng Gao
高敏恆
spellingShingle Min-Heng Gao
高敏恆
Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation
author_sort Min-Heng Gao
title Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation
title_short Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation
title_full Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation
title_fullStr Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation
title_full_unstemmed Study on Applying Anti-corrosion Materials to Diesel-Engine for Biogas Power Generation
title_sort study on applying anti-corrosion materials to diesel-engine for biogas power generation
publishDate 2014
url http://ndltd.ncl.edu.tw/handle/44666390484750273937
work_keys_str_mv AT minhenggao studyonapplyinganticorrosionmaterialstodieselengineforbiogaspowergeneration
AT gāomǐnhéng studyonapplyinganticorrosionmaterialstodieselengineforbiogaspowergeneration
AT minhenggao yùnyòngkàngfǔshícáiliàoyúcháiyóuyǐnqíngjìnxíngzhǎoqìfādiànzhīyánjiū
AT gāomǐnhéng yùnyòngkàngfǔshícáiliàoyúcháiyóuyǐnqíngjìnxíngzhǎoqìfādiànzhīyánjiū
_version_ 1718410254848360448