Control of acoustics and store separation in a cavity in supersonic flow

Thesis (Ph. D.)--Massachusetts Institute of Technology, Dept. of Aeronautics and Astronautics, 2005. === Includes bibliographical references (p. 137-140). === The supersonic flight community is currently faced with two cavity-under-cross-flow related problems, one being the high noise levels inside...

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Bibliographic Details
Main Author: Sahoo, Debashis, 1976-
Other Authors: Anuradha M. Annaswamy.
Format: Others
Language:English
Published: Massachusetts Institute of Technology 2007
Subjects:
Online Access:http://dspace.mit.edu/handle/1721.1/28915
http://hdl.handle.net/1721.1/28915
id ndltd-MIT-oai-dspace.mit.edu-1721.1-28915
record_format oai_dc
collection NDLTD
language English
format Others
sources NDLTD
topic Aeronautics and Astronautics.
spellingShingle Aeronautics and Astronautics.
Sahoo, Debashis, 1976-
Control of acoustics and store separation in a cavity in supersonic flow
description Thesis (Ph. D.)--Massachusetts Institute of Technology, Dept. of Aeronautics and Astronautics, 2005. === Includes bibliographical references (p. 137-140). === The supersonic flight community is currently faced with two cavity-under-cross-flow related problems, one being the high noise levels inside the cavity and the other being the return of a store into the cavity after being released from inside. This thesis provides a systematic framework to understand the dominant physics in both problems and to provide solutions for ameliorating the problems. For the first problem, an innovative cavity acoustics model is developed that rigorously explains the role of leading edge microjets in cavity noise suppression and predicts the magnitude of noise reduction for a given control input (that is the steady pressure at which the microjets are fired). The model is validated through comparison of its noise reduction predictions with experiments done using the Florida State University cavity and wind tunnel for different microjet pressures and under Mach 2.0 and Reynolds number 3 million flow, with the microjets being of diameter 400 microns. Based on the cavity acoustics model, optimization of the control input is performed for microjet-based noise suppression of a general cavity under external cross-flow. The resulting control strategy for the FSU cavity is that of an open loop steady microjet firing with the pressure being uniform along the leading edge. This corresponds to a noise reduction of 9 dB OASPL and 20 dB SPL at the dominant tone. The cavity also exhibits saturation in noise reduction for microjet pressures higher than 30 psig. The second problem that the thesis is concerned with, is that of unsuccessful store drops from an external bay of an aircraft in flight. A group of researchers under the DARPA-funded HIFEX Program is currently developing an effective control mechanism to ensure safe release === (cont.) of a slender axi-symmetric store from a rectangular cavity under supersonic external cross-flow. The actuator being tested under this program is based on a tandem array of microjet flow injectors distributed in the spanwise direction near the leading edge of the cavity, and the control input is the steady pressure levels at which the microjets are fired. In order to optimize the control input to ensure safe store departure, a low order model that reliably predicts the trend in the store drop trajectory in the presence of microjets becomes necessary. In this thesis, a suitable low-order model is developed with separate components to predict the pitch and plunge motion of the store when it is inside the cavity, when it is passing through the shear layer at the mouth of the cavity and when it is completely outside the cavity. The model is based on slender axi-symmetric body aerodynamics, thin shear layer at the cavity mouth, high Reynolds number external cross-flow, plane shock waves associated with the microjet actuators, no-flow condition inside the cavity and inconsideration of the cavity acoustic field. The model is validated by comparing with the results of store drop experiments performed under the HIFEX Program at Mach 2.0 and 2.46 using a generic sub-scale weapons bay for different control inputs. The store drop was observed experimentally and predicted by the model to fail when microjets were switched off and successful with microjets on. However, with an increase in microjet pressure, the store drop became unsuccessful ... === by Debashis Sahoo. === Ph.D.
author2 Anuradha M. Annaswamy.
author_facet Anuradha M. Annaswamy.
Sahoo, Debashis, 1976-
author Sahoo, Debashis, 1976-
author_sort Sahoo, Debashis, 1976-
title Control of acoustics and store separation in a cavity in supersonic flow
title_short Control of acoustics and store separation in a cavity in supersonic flow
title_full Control of acoustics and store separation in a cavity in supersonic flow
title_fullStr Control of acoustics and store separation in a cavity in supersonic flow
title_full_unstemmed Control of acoustics and store separation in a cavity in supersonic flow
title_sort control of acoustics and store separation in a cavity in supersonic flow
publisher Massachusetts Institute of Technology
publishDate 2007
url http://dspace.mit.edu/handle/1721.1/28915
http://hdl.handle.net/1721.1/28915
work_keys_str_mv AT sahoodebashis1976 controlofacousticsandstoreseparationinacavityinsupersonicflow
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spelling ndltd-MIT-oai-dspace.mit.edu-1721.1-289152019-05-02T16:24:25Z Control of acoustics and store separation in a cavity in supersonic flow Sahoo, Debashis, 1976- Anuradha M. Annaswamy. Massachusetts Institute of Technology. Dept. of Aeronautics and Astronautics. Massachusetts Institute of Technology. Dept. of Aeronautics and Astronautics. Aeronautics and Astronautics. Thesis (Ph. D.)--Massachusetts Institute of Technology, Dept. of Aeronautics and Astronautics, 2005. Includes bibliographical references (p. 137-140). The supersonic flight community is currently faced with two cavity-under-cross-flow related problems, one being the high noise levels inside the cavity and the other being the return of a store into the cavity after being released from inside. This thesis provides a systematic framework to understand the dominant physics in both problems and to provide solutions for ameliorating the problems. For the first problem, an innovative cavity acoustics model is developed that rigorously explains the role of leading edge microjets in cavity noise suppression and predicts the magnitude of noise reduction for a given control input (that is the steady pressure at which the microjets are fired). The model is validated through comparison of its noise reduction predictions with experiments done using the Florida State University cavity and wind tunnel for different microjet pressures and under Mach 2.0 and Reynolds number 3 million flow, with the microjets being of diameter 400 microns. Based on the cavity acoustics model, optimization of the control input is performed for microjet-based noise suppression of a general cavity under external cross-flow. The resulting control strategy for the FSU cavity is that of an open loop steady microjet firing with the pressure being uniform along the leading edge. This corresponds to a noise reduction of 9 dB OASPL and 20 dB SPL at the dominant tone. The cavity also exhibits saturation in noise reduction for microjet pressures higher than 30 psig. The second problem that the thesis is concerned with, is that of unsuccessful store drops from an external bay of an aircraft in flight. A group of researchers under the DARPA-funded HIFEX Program is currently developing an effective control mechanism to ensure safe release (cont.) of a slender axi-symmetric store from a rectangular cavity under supersonic external cross-flow. The actuator being tested under this program is based on a tandem array of microjet flow injectors distributed in the spanwise direction near the leading edge of the cavity, and the control input is the steady pressure levels at which the microjets are fired. In order to optimize the control input to ensure safe store departure, a low order model that reliably predicts the trend in the store drop trajectory in the presence of microjets becomes necessary. In this thesis, a suitable low-order model is developed with separate components to predict the pitch and plunge motion of the store when it is inside the cavity, when it is passing through the shear layer at the mouth of the cavity and when it is completely outside the cavity. The model is based on slender axi-symmetric body aerodynamics, thin shear layer at the cavity mouth, high Reynolds number external cross-flow, plane shock waves associated with the microjet actuators, no-flow condition inside the cavity and inconsideration of the cavity acoustic field. The model is validated by comparing with the results of store drop experiments performed under the HIFEX Program at Mach 2.0 and 2.46 using a generic sub-scale weapons bay for different control inputs. The store drop was observed experimentally and predicted by the model to fail when microjets were switched off and successful with microjets on. However, with an increase in microjet pressure, the store drop became unsuccessful ... by Debashis Sahoo. Ph.D. 2007-10-22T16:18:32Z 2007-10-22T16:18:32Z 2005 2005 Thesis http://dspace.mit.edu/handle/1721.1/28915 http://hdl.handle.net/1721.1/28915 60495429 eng M.I.T. theses are protected by copyright. They may be viewed from this source for any purpose, but reproduction or distribution in any format is prohibited without written permission. See provided URL for inquiries about permission. http://dspace.mit.edu/handle/1721.1/28915 http://dspace.mit.edu/handle/1721.1/7582 140 p. application/pdf Massachusetts Institute of Technology