Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZ

<p><span style="font-size: medium;"><span lang="IN">PT. XYZ is a company engaged in the sport shoe with the marketing areas inside and outside the country. One of the products produced by PT. XYZ is running shoes. The problems faced by the company is not achievi...

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Main Authors: andri andri, daniel sembiring
Format: Article
Language:Indonesian
Published: Lembaga Penelitian Universitas Indraprasta PGRI 2019-01-01
Series:Faktor Exacta
Online Access:http://journal.lppmunindra.ac.id/index.php/Faktor_Exacta/article/view/2888
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spelling doaj-dceb4ac8a4b341aaa1a492a85261fc492020-11-24T23:07:47ZindLembaga Penelitian Universitas Indraprasta PGRIFaktor Exacta1979-276X2502-339X2019-01-0111430330910.30998/faktorexacta.v11i4.28882145Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZandri andridaniel sembiring<p><span style="font-size: medium;"><span lang="IN">PT. XYZ is a company engaged in the sport shoe with the marketing areas inside and outside the country. One of the products produced by PT. XYZ is running shoes. The problems faced by the company is not achieving the production targets because many value-added activity not belonging to the waste (waste). For that use lean manufacturing approach to eliminate waste that occurs on in the production line at PT. XYZ. Lean manufacturing methods used is values stream mapping (VSM) to analyze the dominant waste in the manufacturing process. Based on the analysis we found three recommendations for improvement, namely the use of a forklift, the addition operator and addition of machine. Results of evaluation of recommendation is decreased production lead time equal to 8610.62 sec, increasing the value of Process Cycle Efficiency of 21.08%</span><span>.</span></span></p>http://journal.lppmunindra.ac.id/index.php/Faktor_Exacta/article/view/2888
collection DOAJ
language Indonesian
format Article
sources DOAJ
author andri andri
daniel sembiring
spellingShingle andri andri
daniel sembiring
Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZ
Faktor Exacta
author_facet andri andri
daniel sembiring
author_sort andri andri
title Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZ
title_short Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZ
title_full Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZ
title_fullStr Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZ
title_full_unstemmed Penerapan Lean Manufacturing Dengan Metode VSM (Value Sream Mapping) untuk Mengurangi Waste Pada Proses Produksi Pt.XYZ
title_sort penerapan lean manufacturing dengan metode vsm (value sream mapping) untuk mengurangi waste pada proses produksi pt.xyz
publisher Lembaga Penelitian Universitas Indraprasta PGRI
series Faktor Exacta
issn 1979-276X
2502-339X
publishDate 2019-01-01
description <p><span style="font-size: medium;"><span lang="IN">PT. XYZ is a company engaged in the sport shoe with the marketing areas inside and outside the country. One of the products produced by PT. XYZ is running shoes. The problems faced by the company is not achieving the production targets because many value-added activity not belonging to the waste (waste). For that use lean manufacturing approach to eliminate waste that occurs on in the production line at PT. XYZ. Lean manufacturing methods used is values stream mapping (VSM) to analyze the dominant waste in the manufacturing process. Based on the analysis we found three recommendations for improvement, namely the use of a forklift, the addition operator and addition of machine. Results of evaluation of recommendation is decreased production lead time equal to 8610.62 sec, increasing the value of Process Cycle Efficiency of 21.08%</span><span>.</span></span></p>
url http://journal.lppmunindra.ac.id/index.php/Faktor_Exacta/article/view/2888
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AT danielsembiring penerapanleanmanufacturingdenganmetodevsmvaluesreammappinguntukmengurangiwastepadaprosesproduksiptxyz
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