Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernization

The work aims to study the effect of changes in the drain scheme of the low-pressure regeneration on the energy and economic efficiency of the CHP plant-10 power unit No 5 of “Baikal Energy Company” LLC. In this study, we used a mathematical model of the power unit adjusted to the measurements resul...

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Main Authors: Zabuga Fedor, Alekseiuk Vitalii
Format: Article
Language:English
Published: EDP Sciences 2021-01-01
Series:E3S Web of Conferences
Subjects:
Online Access:https://www.e3s-conferences.org/articles/e3sconf/pdf/2021/65/e3sconf_esr2021_02002.pdf
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spelling doaj-b17d27d286284fd19a7dc4799d655d732021-07-15T06:53:43ZengEDP SciencesE3S Web of Conferences2267-12422021-01-012890200210.1051/e3sconf/202128902002e3sconf_esr2021_02002Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernizationZabuga FedorAlekseiuk Vitalii0Melentiev Energy Systems Institute of Siberian Branch of the Russian Academy of SciencesThe work aims to study the effect of changes in the drain scheme of the low-pressure regeneration on the energy and economic efficiency of the CHP plant-10 power unit No 5 of “Baikal Energy Company” LLC. In this study, we used a mathematical model of the power unit adjusted to the measurements results. The mathematical modelling of the power unit was performed using the “Computer-assisted programming system” application package. The created mathematical model of the heat and power plant was tailored to the current state of the study object according to the threestage identification procedure of the mathematical model parameters. We proposed a cycle arrangement under which three streams of the low-pressure drainages were redirected to the pump suction of the low-pressure heater. The improved mathematical model of the power unit allows the calculation of the parameters of both the existing and proposed cycle arrangements. According to the calculations, the temperature difference between the main condensate after the low-pressure heater 1 and the investigated drains after mixing is minimal and amounts to 3.2 °C. The suggested modernisation increases the energy efficiency of the power unit by 0.007% under the nominal operating conditions of the existing and proposed thermal circuit. In addition, the specific standard fuel consumption for electric generation is reduced by 0.052 gram of conventional fuel / kW·h. The operating costs to implement the proposed engineering solutions amounted to 34191 roubles. Considering the annual power plant extensive consumption factor, the payback period of the proposed modernisation will be 5.5 months. The savings for the first operation year are estimated at 18423 roubles, based on the rate of return and depreciation expenses. The proposed approach combines mathematical modelling of operating power plants with a technique of increasing the efficiency of technical decision-making. The proposed versatile approach can be used for the modernisation of CHPs and other plants.https://www.e3s-conferences.org/articles/e3sconf/pdf/2021/65/e3sconf_esr2021_02002.pdfcoal-fired power unitefficiency improvementtechnical solutionmathematical modelingcondensing unitheat flow
collection DOAJ
language English
format Article
sources DOAJ
author Zabuga Fedor
Alekseiuk Vitalii
spellingShingle Zabuga Fedor
Alekseiuk Vitalii
Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernization
E3S Web of Conferences
coal-fired power unit
efficiency improvement
technical solution
mathematical modeling
condensing unit
heat flow
author_facet Zabuga Fedor
Alekseiuk Vitalii
author_sort Zabuga Fedor
title Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernization
title_short Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernization
title_full Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernization
title_fullStr Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernization
title_full_unstemmed Research based on mathematical modeling of CHP-10 power unit No 5 “Baikal Energy Company” LLC to assess the efficiency of its modernization
title_sort research based on mathematical modeling of chp-10 power unit no 5 “baikal energy company” llc to assess the efficiency of its modernization
publisher EDP Sciences
series E3S Web of Conferences
issn 2267-1242
publishDate 2021-01-01
description The work aims to study the effect of changes in the drain scheme of the low-pressure regeneration on the energy and economic efficiency of the CHP plant-10 power unit No 5 of “Baikal Energy Company” LLC. In this study, we used a mathematical model of the power unit adjusted to the measurements results. The mathematical modelling of the power unit was performed using the “Computer-assisted programming system” application package. The created mathematical model of the heat and power plant was tailored to the current state of the study object according to the threestage identification procedure of the mathematical model parameters. We proposed a cycle arrangement under which three streams of the low-pressure drainages were redirected to the pump suction of the low-pressure heater. The improved mathematical model of the power unit allows the calculation of the parameters of both the existing and proposed cycle arrangements. According to the calculations, the temperature difference between the main condensate after the low-pressure heater 1 and the investigated drains after mixing is minimal and amounts to 3.2 °C. The suggested modernisation increases the energy efficiency of the power unit by 0.007% under the nominal operating conditions of the existing and proposed thermal circuit. In addition, the specific standard fuel consumption for electric generation is reduced by 0.052 gram of conventional fuel / kW·h. The operating costs to implement the proposed engineering solutions amounted to 34191 roubles. Considering the annual power plant extensive consumption factor, the payback period of the proposed modernisation will be 5.5 months. The savings for the first operation year are estimated at 18423 roubles, based on the rate of return and depreciation expenses. The proposed approach combines mathematical modelling of operating power plants with a technique of increasing the efficiency of technical decision-making. The proposed versatile approach can be used for the modernisation of CHPs and other plants.
topic coal-fired power unit
efficiency improvement
technical solution
mathematical modeling
condensing unit
heat flow
url https://www.e3s-conferences.org/articles/e3sconf/pdf/2021/65/e3sconf_esr2021_02002.pdf
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AT alekseiukvitalii researchbasedonmathematicalmodelingofchp10powerunitno5baikalenergycompanyllctoassesstheefficiencyofitsmodernization
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